Technical Validation · Hydrocarbons

35-85% Volume Reduction

Oil Sludge Dewatering - Central Chile Refinery

84%
Phenolic Sludge Reduction
77%
Phenols Sludge Reduction
3 months
Technical Validation

Type

Oil Refinery

Industry

Hydrocarbons Refining

Objective

Reduce disposal costs through sludge dewatering

The Challenge

4.5+ million kg/year of oil sludge with high moisture generate excessive transport and disposal costs

High Moisture

70-92% water content

Increases transport weight and volume

High Volume Generated

4.5M kg/year

Three critical process streams

Logistics Costs

Transport + Disposal

Significant OPEX impact

Three Critical Streams

92.59%
Initial Moisture
Phenolic Plant Sludge
Most critical stream
90.02%
Initial Moisture
Phenols Plant Sludge
Second priority stream
70.37%
Initial Moisture
Process Sludge
Third evaluated stream

The Tec-Ionic Solution

Laboratory technical validation without client investment

Innovative Approach

  • No client investment - technical validation with TecIonic equipment
  • Laboratory testing - with industrial-scale equivalent filters
  • Physicochemical characterization - complete for three streams

Applied Technology

  • Mobile vacuum filtration - portable and flexible technology
  • Industrial filter press - real-scale simulation
  • Centrifuge systems - alternative evaluation

5 Additional Opportunities Identified

During the study, applications were identified in Delayed Coker, FCC, effluent treatment, API separators, and storage tanks, expanding the potential impact of mobile filtration technology in the refinery.

Validation Results

Proven volume reduction in three sludge streams

Best Result

Phenolic Plant Sludge

84.23%
Volume Reduction
Initial Moisture
92.59%
Final Moisture
53%

Highest dewatering efficiency achieved

Second Result

Phenols Plant Sludge

77.31%
Volume Reduction
Initial Moisture
90.02%
Final Moisture
56%

Excellent moisture reduction

Third Result

Process Sludge

32.96%
Volume Reduction
Initial Moisture
70.37%
Final Moisture
55.8%

Lower initial moisture, still effective

Global Dewatering Impact

Before Treatment

Annual sludge volume:4.5M kg
Average moisture:70-92%
Disposal cost:High

With Mobile Filtration Technology

Volume reduction:35-85%
Final moisture:53-56%
Disposal cost:Optimized
↓40-85%
Transport trips reduction
53-56%
Optimal final moisture
5
Additional opportunities

Competitive Advantages of the Solution

No Client Investment

Technical validation without capital commitment, reducing financial risk

Mobile Technology

Portable equipment allows operation at multiple refinery points

Logistics Cost Reduction

Lower volume and weight dramatically reduce transport and disposal costs

Potential Water Recovery

Extracted water can be reused in refinery industrial processes

Proven Scalability

20+ years of mining experience applied to the oil sector

Multiple Applications

5 additional opportunities identified in refinery processes

Technical Conclusion

The technical validation performed by Tec-Ionic Durban at this refinery demonstrates the viability of significantly reducing oil sludge volume through mobile filtration technology, with volume reductions ranging from 32.96% to 84.23% depending on the stream.

This solution allows the refinery to evaluate the technology without capital investment, reduce transport and disposal costs, and potentially recover water for reuse. The identification of 5 additional opportunities in different refinery processes expands the potential impact of mobile filtration technology in the oil sector.

84%
Maximum Reduction
53-56%
Final Moisture
3
Validated Streams
5
More Opportunities

Need to Reduce Sludge Disposal Costs?

Our specialists can help you validate dewatering solutions without initial investment, with mobile technology proven in mining and oil sectors.